Added new CONFIG options for the three type of MAC-PHY interconnect and
applied them all relevant board config files
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
SOFT_RESET must be asserted for at least 3 TX clocks. Usually, that's about 30
clock cycles, so it's been mostly working. But we had no guarantee, and at
slower bitrates, it's just over a microsecond (over 1000 clock cycles). This
enforces a 2 microsecond gap between assertion and deassertion.
Signed-off-by: Andy Fleming <afleming@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
100Mbs ethernet does not work on sh7763 chips due to the wrong value being
used in the GECMR register. Following diff fixes the problem
Signed-off-by: Simon Munton <simon@nidoran.m5data.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Driver for Dave DNET ethernet controller (used on Dave/DENX
QongEVB-LITE board).
Signed-off-by: Ilya Yanok <yanok@emcraft.com>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
Modified mii_init to support boards with PHYs that are not set to
autonegotiate, but still want to use u-boot's mii commands to probe
the smi bus. Such PHYs will not set the Autonegotiate-done bit.
Signed-off-by: Richard Retanubun <RichardRetanubun@RuggedCom.com>
Redo how pointers are managed to get rid of ugly casts and strict pointer
aliasing issues that are highlighted by gcc 4.3.
Signed-off-by: Mike Frysinger <vapier@gentoo.org>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
No point in having a Blackfin-specific define "CONFIG_BFIN_MAC_RMII" that
does exactly the same thing as common "CONFIG_RMII".
Signed-off-by: Mike Frysinger <vapier@gentoo.org>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
Rather then defining our own DEBUGF(), just use the common debug().
Signed-off-by: Mike Frysinger <vapier@gentoo.org>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
Rather than having the on-chip MAC hardcoded to phy address 1 and a speed
of 2.5mhz, use these as defaults if the board doesn't specify otherwise.
Signed-off-by: Mike Frysinger <vapier@gentoo.org>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
Cleanup and rewrite the MII/PHY related functions so that we can reuse the
existing common linux/miiphy.h code and hook into the `mii` command.
Signed-off-by: Mike Frysinger <vapier@gentoo.org>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
Rather than hardcoding MDCDIV to 24 (which is correct for ~125mhz SCLK),
use the real algorithm so it gets set correctly regardless of SCLK.
Signed-off-by: Mike Frysinger <vapier@gentoo.org>
Acked-by: Ben Warren <biggerbadderben@gmail.com>
This patch adds support for searching through available PHY-addresses in
the macb-driver. This is needed for the ATEVK1100 evaluation board,
where the PHY-address will be initialized to either 1 or 7.
This patch adds a config option, CONFIG_MACB_SEARCH_PHY, which when
enabled tells the driver to search for the PHY address.
Signed-off-by: Gunnar Rangoy <gunnar@rangoy.com>
Signed-off-by: Paul Driveklepp <pauldriveklepp@gmail.com>
Signed-off-by: Olav Morken <olavmrk@gmail.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This patch adjusts the LED control so that interrupt lines are not reading LEDs
and effectively causing indefinite interrupts to the controller.
Signed-off-by: Ron Madrid <ron_madrid@sbcglobal.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
sh_eth used old network API. This patch changed new API.
Signed-off-by: Nobuhiro Iwamatsu <iwamatsu.nobuhiro@renesas.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This patch changes the reg_read/_write to smc911x_reg_read/_write
and defines then as weak so that they can be overridden by board
specific version.
This will be used by the upcoming VCTH board support.
Signed-off-by: Stefan Roese <sr@denx.de>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This patch tries to ensure that phy interrupt pin
won't be asserted after booting. We experienced
following issues with current 88E1121R phy init:
Marvell 88E1121R phy can be hardware-configured
to share MDC/MDIO and interrupt pins for both ports
P0 and P1 (e.g. as configured on socrates board).
Port 0 interrupt pin will be shared by both ports
in such configuration. After booting Linux and
configuring eth0 interface, port 0 phy interrupts
are enabled. After rebooting without proper eth0
interface shutdown port 0 phy interrupts remain
enabled so any change on port 0 (link status, etc.)
cause assertion of the interrupt. Now booting Linux
and configuring eth1 interface will cause permanent
phy interrupt storm as the registered phy 1 interrupt
handler doesn't acknowledge phy 0 interrupts. This
of course should be fixed in Linux driver too.
Signed-off-by: Anatolij Gustschin <agust@denx.de>
Acked-by: Andy Fleming <afleming@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
All CF platforms' mii.c are consolidated into one
Signed-off-by: TsiChung Liew <Tsi-Chung.Liew@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Also changed path in all linker scripts that reference this driver
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Acked-by: Stefan Roese <sr@denx.de>
Patch to fix buffer allocation size and alignment. Buffer needs to be u32 aligned and
PKTSIZE_ALIGN bytes long.
Acked-by: Michal Simek <monstr@monstr.eu>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Currently VSC8601 doesn't link with 10/100M partners if the
EEPROM/Strapping is not set up.
Setting the auto-neg register fixes this.
Signed-off-by: Andre Schwarz <andre.schwarz@matrix-vision.de>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
get_prom function was used __attriute__ , but it is not enable.
ax88796.o does not do link besides ne2000.o. When ld is carried
out, get_prom function of ax88796.c is ignored.
This problem is a thing by specifications of ld.
I checked and test this patch on SuperH and MIPS.
Signed-off-by: Nobuhiro Iwamatsu <iwamatsu.nobuhiro@renesas.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Fix TBI PHY accesses to use the proper offset in CPU register space. The
previous code would incorrectly access the TBI PHY by reading/writing to CPU
register space at the same location as would be used to access external PHYs.
Signed-off-by: Peter Tyser <ptyser@xes-inc.com>
Acked-by: Andy Fleming <afleming@freescale.com>
The RSK7203 board has the SMSC9118 wired up 'incorrectly'.
Byte-swapping is necessary, and so poor performance is inevitable.
This problem cannot evade by the swap function of CHIP, this can
evade by software Byte-swapping.
And this has problem by FIFO access only. pkt_data_pull/pkt_data_push
functions necessary to solve this problem.
Signed-off-by: Nobuhiro Iwamatsu <iwamatsu.nobuhiro@renesas.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Modified board_eth_init() functions of boards that have this FEC in addition
to other Ethernet controllers.
Affected boards:
bc3450
icecube
mvbc_p
o2dnt
pm520
total5200
tq5200
Removed initialization of controller from net/eth.c
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Affected boards:
hidden_dragon
MPC8544DS
MPC8610HPCN
R2DPLUS
TB0229
Removed initialization of the driver from net/eth.c
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This addresses all drivers whose initializers have already
been moved to board_eth_init()/cpu_eth_init().
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Adds support for configuring the TBI to talk properly with the SerDes.
Signed-off-by: Andy Fleming <afleming@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
The tsec driver contains a hard-coded array of configuration information
for the tsec ethernet controllers. We create a default function that works
for most tsecs, and allow that to be overridden by board code. It creates
an array of tsec_info structures, which are then parsed by the corresponding
driver instance to determine configuration. Also, add regs, miiregs, and
devname fields to the tsec_info structure, so that we don't need the kludgy
"index" parameter.
Signed-off-by: Andy Fleming <afleming@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This is to prepare the way for board code passing in the tsec_info structure
Signed-off-by: Andy Fleming <afleming@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
dm9000 has code to detect and initialize external phy parts, but later
on in the code the part is forced to use the internal phy
unconditionally. Remove the unused/untested code.
change the GPIO initialization so that only the GPIO used as an
internal phy reset (hardwired in the chip) is set as an output. The
remaining GPIO need to be handled by board specific code to prevent
possible drive conflicts. Set as inputs for safety.
replace a few magic numbers with defines
Signed-off-by: Andrew Dyer <adyer@righthandtech.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Add FEC Buffer descriptors and data buffer in SRAM for
faster execution and access.
Signed-off-by: TsiChung Liew <Tsi-Chung.Liew@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
The only board using this driver is the SL8245 board.
Removed initialization for the driver from net/eth.c
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Added board_eth_init() function to bf537-stamp board.
Removed initialization for the Blackin EMAC driver from net/eth.c
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This patch fixes a problem that RTL8110SCL started transfer
with an incorrect memory address.
Signed-off-by: Yoshihiro Shimoda <shimoda.yoshihiro@renesas.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
The received status and len was in little endian
format and caused the ethernet unable to proceed
further. Add __le16_to_cpu() in dm9000_rx_status_8/16/32bit().
Signed-off-by: TsiChung Liew <Tsi-Chung.Liew@freescale.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
This PCI-X e1000 variant works by just adding in the correct
PCI IDs in the appropriate places.
Signed-off-by: Paul Gortmaker <paul.gortmaker@windriver.com>
Remove duplicate definitions in include/lxt971a.h.
Remove duplicate registers and bits definitions in
include/lxt971a.h for standard MII registers, and
use values in include/miiphy.h instead.
Signed-off-by: Hugo Villeneuve <hugo.villeneuve@lyrtech.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Renesas SH7763 has 2 channel Ethernet device.
This is 10/100/1000 Base support.
But this patch check 10/100 Base only.
Signed-off-by: Nobuhiro Iwamatsu <iwamatsu.nobuhiro@renesas.com>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
If enable DEBUG, can not compile ne2000 driver.
Signed-off-by: Nobuhiro Iwamatsu <iwamatsu@nigauri.org>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
According to the Application Notes of the DM9000, only the 2 bits 0:1 of
the status byte need to be checked to identify a valid packet in the fifo
But, The several different Application Notes do not all speak the same
language on these bits. They do not disagree, but only 1 Application Note
noted explicitly that only these 2 bits need to be checked.
Even the datasheets do not mention anything about these 2 bits.
Because the old code, and the kernel check the whole byte, I left this piece
untouched.
However, I tested all board/DM9000[A|E|EP] devices with this 2 bit check, so
it should work.
Notice, that the 2nd iteration through this receive loop (when a 2nd packet is
in the fifo) is much shorter now, compared to the older U-boot driver code,
so that we can maybe run into a hardware condition now that was never seen
before, or maybe was seen very unfrequently.
Additionaly added a cleanup of a stack variable.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
A last minute cleanup before submitting the DM9000A patch series yesterday introduced
a bug in reading the rx-status registers in 32bit mode only.
This patch repairs this.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
Some lines of the U-boot DM9000x driver are longer than 80 characters, or
need some other minor cleanup.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
The DM9000A network controller does not work with the U-boot DM9000x driver.
Analysis showed that many incoming packets are lost.
The DM9000A Application Notes V1.20 (section 5.6.1) recommend that the poll to
check for a valid rx packet be done on the interrupt status register, not
directly by performing the dummy read and the rx status check as is currently
the case in the u-boot driver.
When the recommended poll is done as suggested the driver starts working
correctly on 10Mbit/HD, but on 100MBit/FD packets come in faster so that there
can be more than 1 package in the fifo at the same time.
The driver must perform the rx-status check in a loop and read and handle all
packages until there is no more left _after_ the interrupt RX flag is set.
This change has been tested with DM9000A, DM9000E, DM9000EP.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
According to the application notes of the DM9000 v1.22 chapter 5.2 bullet 2, the
reset procedure must be done twice to properly reset the DM9000 by means of software.
This errata is not needed anymore for the DM9000A, but it does not bother it.
This change has been tested with DM9000A, DM9000E, DM9000EP.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
The eth_send routine of the U-boot DM9000x driver does not match the
DM9000 or DM9000A application notes/programming guides.
This change improves the stability of the DM9000A network controller.
This change has been tested with DM9000A, DM9000E, DM9000EP.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
It seems that the debugging code of the DM9000x driver in U-boot has not been
compiled for a long time, because it cannot compile...
Also rearranged some loglines to get more useful info while debugging.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>
The U-boot DM9000x driver contains a compile time bus-width definition for
the databus connected to the network controller.
This compile check makes the code unclear, inflexible and is unneccessary.
It can be asked to the network controller what its bus-width is by reading bits
6 and 7 of the interrupt status register.
The linux kernel already uses a runtime mechanism to determine this bus-width,
so the implementation below looks somewhat like that implementation.
This change has been tested with DM9000A, DM9000E, DM9000EP.
Signed-off-by: Remy Bohmer <linux@bohmer.net>
Signed-off-by: Ben Warren <biggerbadderben@gmail.com>