DCIMVAC is upgraded to DCCIMVAC for the individual processor
(Cortex-A7) that the DCIMVAC is executed on.
We should follow the linux dma follow. Before DMA read, first
invalidate dcache then after DMA read, invalidate dcache again.
With the DMA direction DMA_FROM_DEVICE, the dcache need be
invalidated again after the DMA completion. The reason is
that we need explicity make sure the dcache been invalidated
thus to get the DMA'ed memory correctly from the physical memory.
Any cache-line fill during the DMA operations such as the
pre-fetching can cause the DMA coherency issue, thus CPU get the stale data.
Signed-off-by: Peng Fan <Peng.Fan@freescale.com>
Signed-off-by: Ye.Li <B37916@freescale.com>
Signed-off-by: Nitin Garg <nitin.garg@freescale.com>
Signed-off-by: Jason Liu <r64343@freescale.com>
Reviewed-by: Stefano Babic <sbabic@denx.de>
Freescale eMMC44 adapter card uses Micron N2M400FDB311A3CF eMMC
memory. According to the silicon datasheet, secure erase timeout
is 600ms. So increase erase timeout value from 250ms to 600ms.
Signed-off-by: Yangbo Lu <yangbo.lu@freescale.com>
Cc: York Sun <yorksun@freescale.com>
High capacity support is not a host capability, but a device capability
that is queried via the OCR. The flag in the operating conditions
request argument can just be set unconditionally. This matches the Linux
implementation.
[panto] Hand merged and renumbering MMC_MODE_DDR_52MHz.
Signed-off-by: Rob Herring <robh@kernel.org>
Signed-off-by: Pantelis Antoniou <pantelis.antoniou@konsulko.com>
Cc: Pantelis Antoniou <pantelis.antoniou@konsulko.com>
The SD clock could be generated by platform clock or peripheral
clock for some platforms. This patch adds peripheral clock
support for T1024/T1040/T2080. To enable it, define
CONFIG_FSL_ESDHC_USE_PERIPHERAL_CLK.
Signed-off-by: Yangbo Lu <yangbo.lu@freescale.com>
Cc: York Sun <yorksun@freescale.com>
Cc: Pantelis Antoniou <panto@antoniou-consulting.com>
Reviewed-by: York Sun <yorksun@freescale.com>
Add adapter card type identification support by reading
FPGA STAT_PRES1 register SDHC Card ID[0:2] bits. To use this function,
define CONFIG_FSL_ESDHC_ADAPTER_IDENT.
Signed-off-by: Yangbo Lu <yangbo.lu@freescale.com>
Cc: York Sun <yorksun@freescale.com>
Cc: Pantelis Antoniou <panto@antoniou-consulting.com>
[York Sun: resolve conflicts in README.fsl-esdhc]
Reviewed-by: York Sun <yorksun@freescale.com>
Add support of the DDR mode for eSDHC driver.
Enable it for i.MX6 SoC family only.
Signed-off-by: Volodymyr Riazantsev <volodymyr.riazantsev@globallogic.com>
Reviewed-by: York Sun <yorksun@freescale.com>
Some boards cannot do voltage negotiation but need to set the VSELECT
bit forcely to ensure it to work at 1.8V.
This commit adds CONFIG_SYS_FSL_ESDHC_FORCE_VSELECT flag for this use.
Signed-off-by: Otavio Salvador <otavio@ossystems.com.br>
This adds support to switch to 1.8V in case CMD11 succeeds.
Signed-off-by: Otavio Salvador <otavio@ossystems.com.br>
Reviewed-by: Marek Vasut <marex@denx.de>
U-Boot has never cared about the type when we get max/min of two
values, but Linux Kernel does. This commit gets min, max, min3, max3
macros synced with the kernel introducing type checks.
Many of references of those macros must be fixed to suppress warnings.
We have two options:
- Use min, max, min3, max3 only when the arguments have the same type
(or add casts to the arguments)
- Use min_t/max_t instead with the appropriate type for the first
argument
Signed-off-by: Masahiro Yamada <yamada.m@jp.panasonic.com>
Acked-by: Pavel Machek <pavel@denx.de>
Acked-by: Lukasz Majewski <l.majewski@samsung.com>
Tested-by: Lukasz Majewski <l.majewski@samsung.com>
[trini: Fixup arch/blackfin/lib/string.c]
Signed-off-by: Tom Rini <trini@ti.com>
The reset value of "uSDHCx_INT_STATUS_EN" register is changed to 0
on iMX6SX. So the fsl_esdhc driver must update to set the register,
otherwise no state can be detected.
Signed-off-by: Ye.Li <B37916@freescale.com>
for multi instance API we use struct fsl_esdhc_cfg to
pass the clock rate. Do not set f_max from global data,
since this is wrong for multi instance case.
Signed-off-by: Markus Niebel <Markus.Niebel@tq-group.com>
Acked-by: Stefano Babic <sbabic@denx.de>
Tested-by: Eric Nelson <eric.nelson@boundarydevices.com>
Reviewed-by: York Sun <yorksun@freescale.com>
For LS1, esdhc is big-endian IP. Accessing the registers
should be in big-endian mode. So we use esdhc_read32()
to read Host controller capabilities register for LS1.
For LS1, when using CMD12, cmdtype need to be set to
ABORT, otherwise, next read command will hang.
Signed-off-by: Alison Wang <alison.wang@freescale.com>
In 7168977 we made calls to check_and_invalidate_dcache_range()
conditional on !CONFIG_SYS_FSL_ESDHC_USE_PIO. Only define this function
in this case as well.
Signed-off-by: Tom Rini <trini@ti.com>
When configure the fsl_esdhc driver to PIO mode by defining
"CONFIG_SYS_FSL_ESDHC_USE_PIO", the SD/MMC read and write will fail.
Two bugs in the driver to cause the issue:
1. The read buffer was invalidated after reading from DATAPORT register,
which should be only applied to DMA mode. The valid data in cache was
overwritten by physical memory.
2. The watermarks are not set in PIO mode, will cause according state not
be set.
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Signed-off-by: Ye.Li <B37916@freescale.com>
T4240RDB board Specification
----------------------------
Memory subsystem:
6GB DDR3
128MB NOR flash
2GB NAND flash
Ethernet:
Eight 1G SGMII ports
Four 10Gbps SFP+ ports
PCIe:
Two PCIe slots
USB:
Two USB2.0 Type A ports
SDHC:
One SD-card port
SATA:
One SATA port
UART:
Dual RJ45 ports
Signed-off-by: Chunhe Lan <Chunhe.Lan@freescale.com>
[York Sun: fix CONFIG_SYS_QE_FMAN_FW_ADDR in T4240RDB.h]
1. The Data timeout counter value in eSDHC_SYSCTL register is
not working as it should be, so add quirks to enable this
workaround to fix it to the max value 0xE.
2. Add CONFIG_SYS_FSL_ERRATUM_ESDHC111 to enable its workaround.
* Update of patch for change mmc interface by
Pantelis Antoniou <panto@antoniou-consulting.com>
Signed-off-by: Haijun Zhang <Haijun.Zhang@freescale.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
The controller reset is performed now if command error occurs.
This commit adds the reset for the case of data related errors too.
Signed-off-by: Andrew Gabbasov <andrew_gabbasov@mentor.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Calculation of the timeout value should be based on actual clock value,
written to controller registers. Since mmc->tran_speed is either the
maximum allowed speed, or the preliminary value, that is be not yet
set to registers, the actual timeout, taken by the controller, based
on its clock settings, may be much longer than expected, based on
mmc->tran_speed value. In particular it happens at early initialization
stage, when typical value of mmc->tran_speed is 20MHz or 26MHz, while
actual clock setting, configured in the controller, is 400kHz.
It's more correct to use mmc->clock value for timeout calculation instead.
Signed-off-by: Andrew Gabbasov <andrew_gabbasov@mentor.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
The way that struct mmc was implemented was a bit of a mess;
configuration and internal state all jumbled up in a single structure.
On top of that the way initialization is done with mmc_register leads
to a lot of duplicated code in drivers.
Typically the initialization got something like this in every driver.
struct mmc *mmc = malloc(sizeof(struct mmc));
memset(mmc, 0, sizeof(struct mmc);
/* fill in fields of mmc struct */
/* store private data pointer */
mmc_register(mmc);
By using the new mmc_create call one just passes an mmc config struct
and an optional private data pointer like this:
struct mmc = mmc_create(&cfg, priv);
All in tree drivers have been updated to the new form, and expect
mmc_register to go away before long.
Changes since v1:
* Use calloc instead of manually calling memset.
* Mark mmc_register as deprecated.
Signed-off-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Using an array is pointless; even more pointless (and scary) is using
sprintf to fill it without a format string.
Signed-off-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Remove the in-structure ops and put them in mmc_ops with
a constant pointer to it.
This makes the mmc structure smaller as well as conserving
code space (in theory).
All in-tree drivers are converted as well; this is done in a
single patch in order to not break git bisect.
Changes since V1:
Fix compilation b0rked issue on omap platforms where OMAP_GPIO was
not set.
Signed-off-by: Pantelis Antoniou <panto@antoniou-consulting.com>
The upper 4 data signals of esdhc are shared with spi flash.
So detect if the upper 4 pins are assigned to esdhc before
enable sdhc 8 bit width.
Signed-off-by: Haijun Zhang <haijun.zhang@freescale.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Reviewed-by: York Sun <yorksun@freescale.com>
Card detection pin is ineffective on T4240QDS Rev1.0.
There are two cards can be connected to board.
1. eMMC card is built-in board, can not be removed. so
For eMMC card it is always there.
2. Card detecting pin is functional for SDHC card in Rev2.0.
This workaround force sdhc driver scan and initialize the card
regardless of whether the card is inserted or not in case Rev1.0.
Signed-off-by: Haijun Zhang <Haijun.Zhang@freescale.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Reviewed-by: York Sun <yorksun@freescale.com>
T4240QDS eSDHC host capabilities reigster should have VS33 bit define.
Add quirk CONFIG_SYS_FSL_MMC_HAS_CAPBLT_VS33 to deal with capacity
missing
Signed-off-by: Roy Zang <tie-fei.zang@freescale.com>
Signed-off-by: Haijun Zhang <Haijun.Zhang@freescale.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
struct mmc should be clear to all '0' after malloc to avoid
unexpect variable value.
Like mmc->has_init = xxx.
In this case mmcinfo will believe the card had been initialized before
and skip the initialization.
Test on P5040 and T4240,
Error Log:
=> mmcinfo
Device: FSL_SDHC
Manufacturer ID: 0
OEM: 0
Name: Tran Speed: 0
Rd Block Len: 0
MMC version 0.0
High Capacity: No
Capacity: 0 Bytes
Bus Width: 0-bit
=>
Signed-off-by: Haijun Zhang <Haijun.Zhang@freescale.com>
Signed-off-by: Xie Shaohui-B21989 <B21989@freescale.com>
Tested-by: Ryan Barnett <rjbarnet@rockwellcollins.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
eSDHC host controller has new register to support SD Spec 3.0.
And the according host controller version was Freescale eSDHC
Version 3.0.
Signed-off-by: Haijun Zhang <haijun.zhang@freescale.com>
Acked-by: Pantelis Antoniou <panto@antoniou-consulting.com>
Dealing with the sys ctrl register should touch only the
relevant bits and not accidently the whole register. On i.MX6,
the sys control register contains bits which shouldn't be reset to
0, e.g. SYS_CTRL[3-0] and IPP_RST_N (SYS_CTRL[23]).
Do this by read/modify/write instead of just a 32bit write.
Signed-off-by: Dirk Behme <dirk.behme@de.bosch.com>
Acked-by: Stefano Babic <sbabic@denx.de>
Signed-off-by: Andy Fleming <afleming@freescale.com>
Fill the right command type when using CMD12 to stop data transfer.
Signed-off-by: Haijun Zhang <Haijun.Zhang@freescale.com>
CC: Fleming Andrew-AFLEMING <AFLEMING@freescale.com>
CC: Scott Wood <scottwood@freescale.com>
Signed-off-by: Andy Fleming <afleming@freescale.com>
After waiting for the command completion event, the interrupt status
bits, that occured to be set by that time, are cleared by writing them
back. It is supposed, that it should be command related bits (command
complete and may be command errors).
However, in some cases the DMA already completes by that time before
the full transaction completes. The corresponding DINT bit gets set
and then cleared before even entering the loop, waiting for data part
completion. That waiting loop never gets this bit set, causing the
operation to hang. This is reported to happen, for example, for write
operation of 1 sector to upper area (block #7400000) of SanDisk Ultra II
8GB card.
The solution could be to explicitly clear only command related interrupt
status bits. However, since subsequent processing does not rely on
any command bits state, it could be easier just to remove clearing
of any bits at that point, leaving them all until all data processing
completes. After that the whole register will be cleared at once.
Also, on occasion, interrupts masking moved to before writing the command,
just for the case there should be no chance of interrupt between the first
command and interrupts masking.
Reported-by: Dirk Behme <dirk.behme@de.bosch.com>
Signed-off-by: Andrew Gabbasov <andrew_gabbasov@mentor.com>
Acked-by: Dirk Behme <dirk.behme@de.bosch.com>
Signed-off-by: Andy Fleming <afleming@freescale.com>
Since commit 48e0b2bd (powerpc/esdhc: Correct judgement for DATA PIO mode)
we see mx6 systems to hang after doing a 'save' command.
Revert this commit since the original 'ifdef' logic from 7b43db92
(drivers/mmc/fsl_esdhc.c: fix compiler warnings) was the correct one.
Reported-by: Tapani Utriainen <tapani@technexion.com>
Signed-off-by: Fabio Estevam <fabio.estevam@freescale.com>
Signed-off-by: Andy Fleming <afleming@freescale.com>
The logic for the whether to configure for polling or DMA
was mistakenly reversed in this patch:
Commit 7b43db9211
drivers/mmc/fsl_esdhc.c: fix compiler warnings
Signed-off-by: Haijun Zhang <Haijun.Zhang@freescale.com>
CC: Sun Yusong-R58495 <yorksun@freescale.com>
Signed-off-by: Andy Fleming <afleming@freescale.com>
A malloc() followed by memset() can be simply replaced by calloc().
Signed-off-by: Fabio Estevam <fabio.estevam@freescale.com>
Signed-off-by: Andy Fleming <afleming@freescale.com>
Rework the waiting for transfer completion loop condition
to continue waiting until both Transfer Complete and DMA End
interrupts occur. Checking of DLA bit in Present State register
looks not needed in addition to interrupts status checking,
so it can be removed from the condition. Also, DMA Error
condition is added to the list of data errors, checked in the loop.
Signed-off-by: Andrew Gabbasov <andrew_gabbasov@mentor.com>
The cache should invalidate the read buffer for
the SD card interface after the transfer complete,
not command-complete.
Tested-by: Andrew Gabbasov <Andrew_Gabbasov@mentor.com>
Signed-off-by: Eric Nelson <eric.nelson@boundarydevices.com>
Maximum bus width supported by some i.MX6 boards is not 8bit like
others. In case where both host controller and card support 8bit transfers,
they agree to communicate on 8bit interface while some boards support only 4bit interface.
Due to this reason the mmc 8bit default mode fails on these boards. To rectify this,
define maximum bus width supported by these boards (4bit). If max_bus_width is not
defined, it is 0 by default and 8bit width support will be enabled in host
capabilities otherwise host capabilities are modified accordingly.
It is tested with a MMCplus card.
Signed-off-by: Abbas Raza <Abbas_Raza@mentor.com>
cc: stefano Babic <sbabic@denx.de>
cc: Andy Fleming <afleming@gmail.com>
Acked-by: Dirk Behme <dirk.behme@de.bosch.com>
Acked-by: Andrew Gabbasov <andrew_gabbasov@mentor.com>
All esdhc variants we know should support high capacity MMC cards,
so let's add MMC_MODE_HC host_caps unconditionally to support those
MMC cards (capacity > 2 GB).
Signed-off-by: Shawn Guo <shawn.guo@linaro.org>